New Advice. Multiple cylinder misfire.
I can start it but it barely revs up, almost like a whole bank just stopped working. I'm not sure where to start, it seems to be affecting Bank 1 or 2 since it would still run or 4-5 cylinders, now it feels like its running on 3. Any help would be appreciated.
Xentry is telling me to do a leak down test on all cylinders, did all my valves just bend?
Last edited by W204Motorsports; Mar 8, 2020 at 04:33 PM.
timing marks are shown in the first minute of this video
On the engine I was working on, checking the timing marks lead me to this discovery. The drivers side exhaust cam pulse wheel (right side of pic) had a big piece break off. When I found the piece it had the impression of the gears between the intake and exhaust cam adjuster so it looked like part of it got caught in between them. That whole event damaged the exhaust actuator internally (all the teeth were fine though somehow) and the actuation was jammed in one direction so I swapped that and the car ran great, there is a bad noise on start up that goes away and an engine light that is triggered in 2 start ups so I am sure the intake adjuster is internally damaged also but I would have to take off the timing chain to swap that one out. Its a 197k miles parts car that had a lot of metal shavings in the oil so thats as far as I will go on that engine
timing marks are shown in the first minute of this video
https://www.youtube.com/watch?v=_Umk-eHegQQ
On the engine I was working on, checking the timing marks lead me to this discovery. The drivers side exhaust cam pulse wheel (right side of pic) had a big piece break off. When I found the piece it had the impression of the gears between the intake and exhaust cam adjuster so it looked like part of it got caught in between them. That whole event damaged the exhaust actuator internally (all the teeth were fine though somehow) and the actuation was jammed in one direction so I swapped that and the car ran great, there is a bad noise on start up that goes away and an engine light that is triggered in 2 start ups so I am sure the intake adjuster is internally damaged also but I would have to take off the timing chain to swap that one out. Its a 197k miles parts car that had a lot of metal shavings in the oil so thats as far as I will go on that engine
Well if you need camshafts I still mine laying around I can donate, they had no damage but if you're saying there's metal in the oil and with close to 200k miles, its obviously not worth fixing when there are so many low mileage units available. I never really figured out exactly what was wrong with it, I still have the engine sitting apart and the only thing left is to remove the cylinder heads and inspect cylinder 4. Mine had similar mileage when it failed and I didn't have time to mess around with it at the time nor was it cost-effective when there was a 2012 3.5L with 50k miles from a glk350 available at my local scrapyard for 1000$. I put over 20k on the 3.5 since and its definitely a nice upgrade.
Last edited by W204Motorsports; Dec 19, 2020 at 04:40 PM.



