HELP: Dealer can't diagnose - Bad Idle/Bucking at Light
There are threads about bad injectors leaking and causing a backfire that can crack the intake manifold.
This is classic vacuum leak symptoms.
I was experiencing the same problem described in your post. Random bucking/surging at idle, the car ran fine above 1000 rpms. I took the car to my mechanic and they could not replicate the problem. One month later, car was due for service and I had all the plugs and wires changed. Problem solved. Car now runs like new.
Good luck.
After changes to ECM (they then had to put the old one back in at no charge because that was not the problem), plugs, Ignition cables... etc... which helped somewhat with the bad bucking at the light... final issue (missing/shudder while idling) was resolved by EGR valve.. replacement.
Technically the car was at the dealer from April 11th until May 4th!
Thanks to all... Just glad I have it back. My biggest dissapointment in the whole process was the dealer was in a hurry to discharge the car after bucking was fixed but the rough idle was not... I think I burnt some bridges there... Service Manager did jump in and save the day in the end.
This has been a nightmare...
hopefully this fixes my issue so i can throw the old egr valve in his face
Desired speeds , changed his out and it still does it .. not sure if i should pick one up or not now ..
Too bad. I suggested the vacuum be checked back on May 2nd. Apparently they did not do this.
Last edited by Schweinhund; May 19, 2011 at 06:06 PM.

To the OP: Glad that you got your car back, and it's repaired correctly (finally).
Last edited by cudaized; May 19, 2011 at 09:13 PM.
The Best of Mercedes & AMG
Nick
now that thing is rough.
After changes to ECM (they then had to put the old one back in at no charge because that was not the problem), plugs, Ignition cables... etc... which helped somewhat with the bad bucking at the light... final issue (missing/shudder while idling) was resolved by EGR valve.. replacement.
Technically the car was at the dealer from April 11th until May 4th!
Thanks to all... Just glad I have it back. My biggest dissapointment in the whole process was the dealer was in a hurry to discharge the car after bucking was fixed but the rough idle was not... I think I burnt some bridges there... Service Manager did jump in and save the day in the end.
This has been a nightmare...
EGR eh
Interesting indeed. You would think with all the high end data equipment they would have found the issue a lot sooner than later. However problem fixed!
Welcome back







