bouncing idle
When you first start it, idles normally, then with a tap on the throttle it goes into surge mode.
Throttle ecu reset does not solve.
TB was clean, took it off and cleaned it anyway. No signs of bad tb wires, no change when wiggled anyway. When I unplug the tb it gets a more intense/rapid bounce and idles up.
No vacuum leaks apparent.
Fuel pressure is steady at ~55psi
After I tested the fuel pressure the problem went away, for now. It was a sporadic problem last week.
Any ideas? I can't be the first to experience it.
When you first start it, idles normally, then with a tap on the throttle it goes into surge mode.
Throttle ecu reset does not solve.
TB was clean, took it off and cleaned it anyway. No signs of bad tb wires, no change when wiggled anyway. When I unplug the tb it gets a more intense/rapid bounce and idles up.
No vacuum leaks apparent.
Fuel pressure is steady at ~55psi
After I tested the fuel pressure the problem went away, for now. It was a sporadic problem last week.
Any ideas? I can't be the first to experience it.
sounded like 'wroom.....wroom.....wroom....wroom' around 1500rpm oscillating in about 0.5s
(hard to write soundeffects on foreign language
)
Trending Topics
Get it scanned and see if there are any stored codes or events.
Possible its the fuel pressure regulator as stated above, which is an integrated part of the fuel filter on the C32. Easy replacement, give it a shot. Still stumbling afterwards, maybe time to check injector spray patterns... maybe an injector is clogged or malfunctioning?
Also just bouncing it out there, it's a possibility there is an issue with the ECU. Is there oil in your engine wiring harness by chance?
Validity
Engines M112, M113
Power generation / Engine management / Engine running / Stalls/goes out
Power generation / Engine management / Engine running / Surges
Power generation / Engine management / Engine running / Cuts out intermittently
Power generation / Engine management / Engine running / Runs rough/shakes
ME-SFI-Motor electronics (MESE) (CLK (209),C (203),E (211),SLK (171))
Last edited by Supgee; Sep 24, 2014 at 09:24 PM.
The Best of Mercedes & AMG
Supercharged engines have a MAP not MAF. Cheap enough part I'll replace that if the fuel filter doesn't solve it.
ECU harness ok.
I've run a can of mb fuel cleaner through about 10k mi ago, I'm at 150k now, plenty of power when I'm not experiencing this. I would imagine a stuck injector would be a constant.
No engine codes but I'll get it scanned for fun. Can I use star to look at throttle pedal output?
It is not a constant problem but has happened a few times in the last few months. Every once and a while it will be noticeable but not extreme, just a little bounce off idle about 50 rpms instead of 500.
1.with car running and idling up and down sprayed carb cleaner around air intake at the rear where the two rubber gators go over the filters to the air intake throttle body. Every now and again idle would even out, this proved that there was some air leaks around the rubber intake boots.
2.After some real close inspection I also found the air breather tubes from the valve covers had a small crack due to hardening on the underside.
3.I purchased a new air intake adaptor with the two rubber boots and at the same the two rubber hose connects to the valve covers.
4.Took all filter off cleaned everything, cleaned the throttle body, it was real dirty. Re fitted the new hoses to valve covers , this is a little awkward, fitted to air intake boot assembly again this was not easy needs some patience DID not have the steel clamp bands so used black wire ties. you can't see them so looks great.
5.Started up and idle is great no hunting or ups and downs.
6. It was very hard to see any leeks so you need to us carb cleaner and spray around air intake area and my engine evened out and then starting to "hunt" again this is how I found the leaks
Hope this helps.
John

I replaced #4 and the the two hoses on the valve covers that connect to underside of air intake. also look carefully at airline that comes into back side of throttle body , mine was not pushed in properly, it may have got moved when somebody fitted new filters









