Porting, Polishing, and Cams project
software, Magnecor Wires, IK20's, K&N filters & I make
295rwhp & 309rwtq which equates to 357HP & 374TQ
There's one particular car that really has my attention, he has
his C32 in a drifting stance in his signature, makes 317rwhp &
327rwtq on ASP pullies and Renntech software, I forgot his
screen name for the moment, it's too early for me to be thinking
in the morning.
software, Magnecor Wires, IK20's, K&N filters & I make
295rwhp & 309rwtq which equates to 357HP & 374TQ
There's one particular car that really has my attention, he has
his C32 in a drifting stance in his signature, makes 317rwhp &
327rwtq on ASP pullies and Renntech software, I forgot his
screen name for the moment, it's too early for me to be thinking
in the morning.
I guess you'll be on the list for a LET pulley if it makes the right numbers.
software, Magnecor Wires, IK20's, K&N filters & I make
295rwhp & 309rwtq which equates to 357HP & 374TQ
There's one particular car that really has my attention, he has
his C32 in a drifting stance in his signature, makes 317rwhp &
327rwtq on ASP pullies and Renntech software, I forgot his
screen name for the moment, it's too early for me to be thinking
in the morning.
I hate to say it, but it looks like you are having the same issue as me. Take a look at your graph from Lujan. At 4800 RPM you can see that the car is holding power back.
members here in South FL with Renntech C32's. I want to see
the data log my CarChip Pro to scan it. Jerry said my car makes
more boost than his with the LET pulley kit, so I want to see
that first hand and then I'll go from there.
Honson? Donn? Where are you guys?
There's been alot of officers where I go test out my cars and
I don't need a $300+ ticket anytime soon

PS at 362rwhp you were at 438BHP!
At 4400 RPM something happened and your car continues to pull power to red line. I bet your car is pulling timing to the tune of -21 to -30.
We both have the IK-20 plugs, magnecor wires, and Renntech tuning.
The Best of Mercedes & AMG
i am going to do some datalogging this afternoon...i will let you know what happens
shots.
P&L regapped the plugs to 32 and the car runs much better. The shift from 1st to 2nd is very noticeable now.
The leak down test results were:
155 PSI across the board on the left bank.
165 PSI across the board on the right bank.
Less than 10% leakage across the board.
These numbers are perfect...which kind of makes me mad. This means that we have to look elsewhere.
Erick and I both have Dyno appts on Friday, so expect graphs then.
P&L regapped the plugs to 32 and the car runs much better. The shift from 1st to 2nd is very noticeable now.
I just installed my IK20s and just hand tightened them, then did a 1/2 turn with the wrench.
when i checked the gap before i re-gapped them, they were all at .043-4...ouch!








