*** 208 Prototype ***
My car is sitting at the dealership!!! For some reason they let a tech that had never installed headers or even remove/replace the stock manifolds work on my car.

There are some nuances to installing these types of part (manifolds/headers) that are inherent to MB's.
Here's what happened...
When I picked my car up the first day it was great no issues whatsoever. The next couple of day I here this spitting of air, that sounds like it's coming from underneath the car. It goes away when the engine heats up, but will come back once it's cooled down and you start it again.
My first thought was 'Great, blew the welds on the X-pipe or Y-collector!!' This is Friday afternoon, and I can't get it into the exhaust shop til Monday. I get it there, they take a look and everything's fine. Now I can't get into the dealership until Thursday; drop it off for the tech to look at. That evening the SA gives me a call the tech is saying the flange is warped and that's what's causing the the leak and ask what would I like him to do. I tell hime I would like you to let me speak to the tech; the tech says he has gotten the nut as tight as he dare and there is gap between the flange and the block. He then preceeds to tell me that he even went so far as to remove the nut/stud combo and replace it with a screw. I tell him to leave it and I won't to see what he is talking about.
At this point I shoot off an email to my fabricator and he gives me all the info I need about what he did wrong and what it would take to fix it. As it turns out, sometime when you are remove the manifolds the nut and the stud will come out together. A lot of techs think it's okay to put the put it back in this way as well, however; the proper method is to take the nut off of the stud, reinstall the stud into the block and then you can reuse the nut. Doing it the other way can cause the stud to crossthread and not allow for a good seal. They also sometimes double up on the gaskets or not get them lined up properly.
So when I get there Friday, I go ever my questions he knew nothing about what I just described above. Says he has installed a number of headers, but never on an MB. I look at the stud and you were threads had been flat spotted from not being seated properly in the block. He puts the car up on the lift and sure enough there's this freakin screw waving back at me like...

So now come Monday he has to take it all apart and inspect the stud holes so we can figure out the proper course of action. Needless to say I am not a happy camper!!!

I will post that info on the install when I get back to the office on Monday, and once I find out something I will let you all know.
-Ghost
Last edited by Ghostrider; Aug 25, 2007 at 06:11 PM.
The heat will never warp the flanges we use. We use a water jet cut P&O steel that's flat sanded and trued after all welding is done. Chances are either the tech doubled the gaskets on the back cylinder and bent the flange of the gaskets or when the OEM manifolds were removed, the studs came out when the nuts were being removed.
Most techs believe its ok to not remove the nuts from the studs when reinstalling them. Well because of the flange thickness difference (1/4" to 3/8"); when the stud/nut combo is reinstalled, the holding depth needed for the 6mm stud is no longer there. So this will tend to pull the threads out of the head. The back cylinders are common to have the studs come out when the manifolds are removed.
Every Mercedes that we've done has had this happened. It’s the installation method afterward that makes the difference. The easiest way to tell is if the stud length is the same sticking out past the head of the nuts. If they are not all the same then the stud was not installed properly.
The factory exhaust manifold studs are already a high-carbon hardened steel; this is the same material ARP.
What you need to do is this:
Always tighten the bolts starting at the back of the engine, moving forward- start with the flange closest to the firewall, tighten both nuts, then move forward one flange, tighten the two nuts, etc. -Don't tighten all of the top nuts first, then all of the bottom nuts next- this is likely why you have an exhaust leak at the head. Torqueing from the back to the front will ensure the sealing surface of the header flange is square to the cylinder head on every runner as it is torqued down.
What you need to do is this:
Always tighten the bolts starting at the back of the engine, moving forward- start with the flange closest to the firewall, tighten both nuts, then move forward one flange, tighten the two nuts, etc. -Don't tighten all of the top nuts first, then all of the bottom nuts next- this is likely why you have an exhaust leak at the head. Torqueing from the back to the front will ensure the sealing surface of the header flange is square to the cylinder head on every runner as it is torqued down.
The Best of Mercedes & AMG
The dyno appointment is set for tomorrow at 9:30 in the morning so keep your fingers crossed.
Can't wait for the Dyno results.

So to sum up the vehicle:
208 Prototype HFM
SC Delete
X-pipe/Y-collector
AMG airbox
Evosport pulleys
The car was run with my 19x10's, 265/30-19 Falken FK452. I did not have time to get my stock wheels on before my appointment.
I think the car could use some tuning!!!! Let me know what you think....
I'm hoping some of the dyno readers will chime in and let me know how it looks.
Stephen (SoCalCLK) was seeing 245HP at the rear wheels on a bone stock 2002 CLK430. Another regular poster ran 13.8's @ 102+ MPH on a stock 2002 CLK430. According to my drag calculator, 102+ MPH in a 3500 pound car requires a bit more than 275HP.
Stephen (SoCalCLK) was seeing 245HP at the rear wheels on a bone stock 2002 CLK430. Another regular poster ran 13.8's @ 102+ MPH on a stock 2002 CLK430. According to my drag calculator, 102+ MPH in a 3500 pound car requires a bit more than 275HP.
Hey Marcus, what do the specs say about the 0-60 and 1/4 mile times??
There's a slip at my website from some time ago. Bone stock at Sactown Raceway - 13.88 @ 102.4 MPH with the adaptive throttle reset, the ESP off, and no spare tire or jack.
There's a slip at my website from some time ago. Bone stock at Sactown Raceway - 13.88 @ 102.4 MPH with the adaptive throttle reset, the ESP off, and no spare tire or jack.
I know what I need to do!!!
So.... Without further ado, I present, The Results:
This is my first dyno from a year ago. I had the airbox, filters, and pullies on at this time.
Last edited by Ghostrider; Sep 21, 2007 at 03:59 PM.






